除对极少数凝析气藏采用循环注气方式开采以外,我国对绝大多数凝析气藏均采用衰竭式开采。衰竭式开采采出程度低,大部分资源损失在地下;若不改变这种开采方式就无法再采出剩余的资源。从室内实验和现场试验两个方面进行了凝析气藏注水开采研究。室内实验表明,注水可以提高凝析油采收率3.39%,可提高天然气采收率10.11%。采用油田污水现场回注于废弃气藏证实:截止2003年4月,板桥凝析气藏在累计注水127.06×10~4m~3后新增采油量6 638t、采气量5020×10~4m~3。实践表明:油田污水回注于废弃气藏是老油田挖潜和提高经济效益的一条新途径,并在拓宽凝析气藏的开发方式和提高凝析气藏开发水平方面有理论意义、在增加凝析气藏的油气可采储量和寻求油气藏接替资源方面有现实意义。
程远忠;刘立平;李国江;左松华;张宝红;董治; . 板桥废弃凝析气藏注水提高采收率研究[J]. 天然气地球科学, 2003 , 14(4) : 298 -301 . DOI: 10.11764/j.issn.1672-1926.2003.04.298
Depleted way is main producing method for condesate gas reservoir besids a few kinds of there reservoirs being produced by gas-cycling in China. A big problem of depleting producing is making low condensate oil recovery. Lab experiment and development test on spot have been done in Banqiao oil field. It is show that formation waste water injection is a feasiblity way to improve condensate oil and gas recovery for abandened condensate gas reservoir. More about 3. 39 percent condensate oil and 10. 11 percent .
Key words: Condensated gas reservoir; Depletion; Developing mode; Water injection; Recovery.
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